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generation minus the net trip generation for the existing uses? The method for this calculation was not <br />included/explained in the revised traffic study, and RYE was unable to decipher it from the text of the <br />report. RKE commented that this is significant because it "could affect all of the traffic analysis for the <br />future conditions with the project." Accordingly, the method used to calculate the project only volumes <br />must be clarified so its accuracy and completeness can be evaluated. <br />Fourth, the 2019 revised traffic study is inaccurate because it does not use current data or <br />current conditions in its analysis of the effects of the Russell Fischer Car Wash Project on traffic. RKE <br />identified this inaccuracy several times throughout the study. For instance, the revised traffic study <br />evaluation of near -term traffic conditions was for the year 2019. RKE found that this is not a realistic <br />timeframe, since it is nearly the last quarter of year 2019 and the Car Wash Project has not yet been <br />approved and would need a period for construction. Accordingly RKE found that a much later time <br />frame should be evaluated for near -term conditions, and suggests an Opening Year of 2020 or 2021. <br />Similarly, the near -term traffic analysis shown on page 3-91 needs to be a more realistic year than Year <br />2019, since Year 2019 is nearly over. <br />The traffic counts mentioned on page 3-72 of the revised traffic study were taken in October of <br />2016, three years ago, even though the revised traffic study was prepared in 2019. RKE found that the <br />revised traffic study should have been updated with more current traffic counts in 2019 to reflect <br />existing conditions. The outdated traffic counts affect the overall analysis of whether the Russell <br />Fischer Car Wash Project has a significant impact on traffic. <br />Moreover, the revised traffic study for the Russell Fischer Car Wash Project tools a trip credit for <br />the traffic from the sit-down restaurant building that used to exist on the site at 301 N. Tustin Avenue. <br />RK Engineering found that this would only be valid if the restaurant was in full operation when the <br />traffic counts were taken. Nonetheless, the restaurant closed and the building has been cleared from the <br />site. Since the 2016 traffic counts used in the revised traffic study should be updated to reflect 2019 <br />traffic conditions, this restaurant trip credit cannot be utilized. Accordingly, the trip counts used in the <br />revised traffic study are inaccurate. <br />Lastly, as shown on page 3-82, the traffic study used the ITE (Institute of Transportation <br />Engineers) 9th Edition of Trip Generation rates which was published in 2012. This manual was updated <br />in the ITE Trip generation, 10th Edition published in 2017. RK Engineering commented that the latest <br />manual should have been used since both the original traffic study and the 2019 revised traffic study <br />were done significantly after the new ITE Trip Generation data was available. Accordingly, on page 3- <br />101, Table 6-2 needs to use the more current ITE loth Edition Trip Generation for all of the cumulative <br />projects. <br />In light of the foregoing, the Russell Fischer Car Wash Project is not categorically exempt from <br />CEQA review as an infill development project because the traffic study is incomplete and outdated, and <br />thus insufficient to support the Planning Commission's determination that the Project will have no <br />significant effects relating to traffic (CEQA § 15332(4)). The review and data provided by RKE shows <br />15 <br />75A-25 <br />